Zax Bugeye "Shaggin' wagon" Build thread by zax

By diyauto
( 2 )

2 minute(s) of a 100 minute read

2-5-2013

2-5-2013


Compression test results:


Cylinder 1:



Cylinder 3:



Cylinder 2:



Cylinder 4:



Motor was only lukewarm, unfortunately. Compression in cylinder 1 dropped a few PSI, but still well within healthy limits. Still excellent compression for a 2003.


149 - 155 - 157 – 152


3-8-2013


Alright, I suppose I should give an update!


I had a local shop perform a full leakdown on the motor and vac leak check. The leakdown results were excellent, with less than 4% loss in each cylinder. The Vac leak check was not so great. Evidently I had vac leaks in hoses, from the TGV-cyl head gaskets, TMIC-TB silicone coupler and a few others. Furthermore, like I suspected, injector 3 was poorly seated in the fuel rail. At least I now know from where the issues arose. Furthermore, I'm excited to hear that my motor is in excellent condition. Since I mentioned I had checked injector #3, I will tell the embarrassing story to anyone who wishes to know via PM.


3-12-2013




Beamed at your face at approx. 186,000 miles per second via DROID BIONIC



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