Turbo LS1 240z Build by sq_creations

By diyauto
( 3 )

3 minute(s) of a 92 minute read

2-11-2010



My buddy is letting me use his go pro camera. Here is a video on the way to work this morning. Couple of 1/3 throttle pulls.


2-16-2010


15~20 or when I run out of fuel. which ever comes first. lol. 


Hoping to get on the dyno thursday. Waiting to here back. I know they are trying to get there shop car ready for some test runs in phoenix this weekend. 


Here is another video that just popped up.




2-19-2010


I’m very happy to be alive right now. The Z burst in to flames last night. The injector on cylinder 8 popped out enough that it sprayed fuel that ignited. The night started off with the dyno acting up. The first few pulls I did would not show any graph. Scottie figured out the speed sensor was being cranky and got it working. So I started doing some tuning. Now the car would hit about 5 psi on the street on wastegate. My past experience is that most cars will be 2~3 psi lower on the dyno. This is my first time playing with a car that has a glide in it on the dyno. I was surprised that the car would only build 0~1psi of boost. After a few runs I got it up too 380whp on like 0.5 psi @ 6500. I think the glide might be robbing some power but what ever. I notice that I need more base fuel pressure after reviewing the logs. I thought I was at 45 but with the car at ldle it was only 30. My pump should be good for 120 so I took the base pressure to 60. I figure at full boost it would be no more that 80psi of fuel pressure. Well get the map dialed in again and then turned up the boost. I went to do a pull and as the boost came on I heard a noise and saw a blanket of fire flowing over the the windshield like a river. Its kind of a blur but I jumped out of the car hit the kill switch and got to the extinguisher and put out the fire. The whole engine bay was a blaze. The room was filled with yellow powder. I went out of the room but saw more flames so I rushed back in to put them out. Now at this point Scottie had left earlier to get us some dinner so I was alone. The visibility was that of a dense fog and the second time coming out of the dyno room I felt myself blacking out so I made the call 911 to see if I had just poisoned myself. As the call progressed I came back too. I had just deplete all my oxygen. About that time Scottie rolled back up. He total helped me call down. Thanks bro you’re a good friend. The end result was like 420 @ 4000 on 3~4 psi. Now its time to rebuild the harness and see else needs to be replaced. I know I need stronger brackets holding the fuel rails. I’m going to go clean up the mess today.



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